- Manufactured
                              Housing Energy Use Study, North Carolina A&T 
 
 
Side-by-side
                      monitoring of two manufactured homes at North Carolina
                      Agricultural and Technical State University (NCA&TSU),
                    evaluated the value of a variety of energy saving technologies
                    and techniques. (Figure 50 and Table 28) Home instrumentation
                    measured energy consumption as well as interior and exterior
                    climatic conditions. The “standard home,” designed
                    and built to basic HUD code requirements, represented the
                    control home. Modified to use at least 50% less energy, the “energy
                    home” met Building America standards. Cooperating researchers
                    at NCA&TSU and FSEC investigated energy feature performance
                    and compared actual energy used to energy modeling program
                    predictions. In-situ energy performance data provided researchers
                    with interesting information on both issues.  
 | 
 
  Figure 50  Side-by-side
                      monitoring of  
                      manufactured homes at NCA&TSU.  | 
 
 
Each
                      model contained 1,528 ft 2 of living area with nearly identical
                      floor plans. Though the homes were unoccupied during the
                      testing, home lighting and water heating use was simulated
                      with timers. A datalogger in each home recorded: (1) the
                      interior and exterior temperature and humidity along with
                      solar radiation and wind speed, (2) the home’s total
                    power consumption, (3) the air conditioning/heat pump compressor,
                    air handler fan, and electric resistance heater use (primary
                    heater in the standard house, backup or emergency heater
                    for the energy house), and (4) water heating and water usage
                  data.  
 The energy house features combined higher insulation values,
                    improved windows, centralized and airtight duct design, high
                    efficiency heat pump, and a solar water heater. Feature-by-feature
                    construction differences are highlighted in Table 28.  
 Table
                          28 Specifications of Standard and Energy Construction  | 
 
 Characteristic  | 
 Standard House  | 
 Building America
                          House  | 
 
 square footage   | 
 1528   | 
 1528   | 
 
 floor insulation   | 
 R-11   | 
 R-22   | 
 
 wall insulation   | 
 R-11   | 
 R-13   | 
 
 ceiling insulation   | 
 R-20   | 
 R-33 + roof deck radiant
                        barrier   | 
 
 windows   | 
 single pane with interior
                        storm   | 
 low-E double pane   | 
 
 exterior doors   | 
 storm door on front   | 
 storm door on all   | 
 
 marriage wall seal   | 
 fiberglass pad   | 
 sof-seal gasket   | 
 
 heating system   | 
 resistance electric   | 
 heat pump HSPF 7.5   | 
 
 cooling system   | 
 central air conditioning
                        SEER10   | 
 central heat pump SEER12   | 
 
 system size   | 
 3 tons   | 
 2 tons   | 
 
 water heating   | 
 electric
                          water heater – 40
                        gallon   | 
 solar
                          water heater – 66
                        gallon   | 
 
 duct joints   | 
 industry standard   | 
 sealed with mastic   | 
 
 duct leakage   | 
 *CFM5out = 145   | 
 CFM25out = 83   | 
 
 house leakage   | 
 **ACH50 = 10   | 
 ACH50 = 9   | 
 
 *Cubic
                          feet per minute 
                          **Air changes per hour   | 
 
 
 Data collection on the two homes began in early January 2001
                  and continued through this reporting period. Palm Harbor Homes
                  in Siler City manufactured both homes, the results for program
                  year three and four are detailed below.  
 Year 4 Side-by-Side Monitoring Results 
 During
                    Phase 2, modifications were made to the solar water heating
                    system in the energy efficient housing unit to help improve
                    the performance this system. Further, a number of the incandescent
                    light bulbs in the energy unit were replaced with compact
                    fluorescent bulbs. These changes were staged to allow an
                    evaluation of the effect of each measure on the home’s
                  energy use.  
 Based on investigative results, it can be concluded that:  
-  Changes
                      in the building envelope, HVAC and duct systems, and fenestrations
                      in the energy home met researchers’ 50%
                    energy use reduction goal. Measured annual energy savings
                    for heating and cooling energy was 58%, and 53% for heating,
                    cooling, and hot water production. 
 
- Care
                        should be exercised in the manufactured housing unit
                      setup or relatively minor construction deficiencies can
                      significantly reduce a home’s energy efficiency.
                        Many of these items are invisible to the homeowner; therefore
                        procedures must be developed to ensure that deficiencies
                    do not occur during setup. 
 
- The
                        Energy Gauge energy analysis program appears to give
                      a reasonably accurate prediction for expected energy use
                        reduction in a typical manufactured housing configuration.
                      The predicted energy savings for the housing units evaluated
                      in this investigation ranged from 54% to 63%, while the
                      measured values ranged from 53% to 58%. Version 2.0 of
                      the Energy Gauge Program provided a more accurate energy
                    savings prediction than the older software versions. 
 
- An
                        increase in pipe and tank insulation can increase not
                      only the energy efficiency of a solar water heater by reducing
                      stand-by losses, but also can reduce the cooling load in
                      a manufactured housing unit and increase the overall energy
                      efficiency of the water heating unit. Even small amounts
                      of exposed piping can significantly affect the energy efficiency
                      of the water heating system. 
 
-  While
                        providing essentially the same lighting levels, replacing
                        incandescent lamps with compact fluorescent bulbs not
                      only reduces lighting energy use, but also reduces the
                      home cooling load. 
 
 
 The total measured energy used by each of the housing units
                  for cooling and heating are shown in tables below. Table
                  29 shows the energy used for heating and cooling the standard
                  housing unit from January through August of 2002. The standard
                  home datalogger was struck by lighting in mid-August 2002.
                  Data after this point was not included since only partial data
                  is available and performance comparisons were not possible. Table
                  30 shows a summary of the cooling and heating energy used
                  by the energy housing unit. Tables 31 and 32 list
                  the energy use for hot water production for the standard and
                  energy units, respectively.  
 Table
                          29 Cooling and Heating Energy Use, Standard House  Actual
                          Values (kWh)  | 
 
 | 
 SEP   | 
 OCT   | 
 NOV   | 
 DEC   | 
 JAN   | 
 FEB   | 
 MAR   | 
 APR   | 
 MAY   | 
 JUN   | 
 JUL   | 
 AUG   | 
 
 Phase
                          1   | 
 492.4   | 
 447.6   | 
 648.6   | 
 1741.1   | 
 2495.3   | 
 849.6   | 
 628.8   | 
 384   | 
 566.3   | 
 990.8   | 
 852.9   | 
 1066   | 
 
 Phase
                          2   | 
 | 
 2120.2   | 
 1717.1   | 
 1227.6   | 
 502.0   | 
 438.0   | 
 939.4   | 
 1079.4   | 
 511.2   | 
 
 
 
 Table
                          30 Cooling and Heating Energy Use, Energy Star House  | 
 
 | 
 SEP   | 
 OCT   | 
 NOV   | 
 DEC   | 
 JAN   | 
 FEB   | 
 MAR   | 
 APR   | 
 MAY   | 
 JUN   | 
 JUL   | 
 AUG   | 
 
 Phase
                          1   | 
 337.3   | 
 205.7   | 
 150.8   | 
 452.8   | 
 1087.3   | 
 472.8   | 
 426.9   | 
 184.8   | 
 528.3   | 
 891.5   | 
 850.9   | 
 671.6   | 
 
 Phase
                          2   | 
 | 
 680.7   | 
 537.1   | 
 378.1   | 
 241.9   | 
 311.8   | 
 603.0   | 
 668   | 
 626.6   | 
 
 
 
 Table
                          31 Domestic Hot Water Use, Standard House  | 
 
 | 
 SEP   | 
 OCT   | 
 NOV   | 
 DEC   | 
 JAN   | 
 FEB   | 
 MAR   | 
 APR   | 
 MAY   | 
 JUN   | 
 JUL   | 
 AUG   | 
 
 Phase
                          1   | 
 197.8   | 
 267.7   | 
 250.2   | 
 212.6   | 
 0   | 
 0   | 
 217.6   | 
 244.9   | 
 258.1   | 
 227.5   | 
 207.9   | 
 213.5   | 
 
 Phase
                          2   | 
 | 
 294.6   | 
 280.9   | 
 283.2   | 
 264.9   | 
 280.2   | 
 192.2   | 
 200.3   | 
 85.2   | 
 
 
 
 Table
                          32 Domestic Hot Water Use, Energy Star House  | 
 
 | 
 SEP   | 
 OCT   | 
 NOV   | 
 DEC   | 
 JAN   | 
 FEB   | 
 MAR   | 
 APR   | 
 MAY   | 
 JUN   | 
 JUL   | 
 AUG   | 
 
 Phase
                          1   | 
 133.4   | 
 176.2   | 
 204.2   | 
 189.9   | 
 0   | 
 0   | 
 245.5   | 
 184.4   | 
 183.0   | 
 141.2   | 
 152.3   | 
 126.6   | 
 
 Phase
                          2   | 
 | 
 251.1   | 
 212.0   | 
 202.8   | 
 145.9   | 
 157.3   | 
 74.8   | 
 80.3   | 
 83.0   | 
 
 
 Also
                    listed in each table are the monthly energy use values measured
                    during the first phase of this investigation, January through
                    August 2001. Please note that the energy housing unit data
                    prior to August 2001 is suspect due to duct and HVAC system
                  problems later corrected. The entire data set, including, temperature,
                  relative humidity, solar radiation, and power use is listed
                  on the FSEC web site www.infomonitors.com.  
 The total energy used for water heating and central cooling
                  over the period of August 1 through August 15 was 363.5 kWh
                  for the energy home and 596 kWh for the standard home. This
                  represents a 40 % reduction in energy use between the two homes.  
 The total energy used over the period of August 1 through
                  August 15 for water heating was 27.13 kWh for the energy house
                  and 85.18 kWh for the standard home. This represents a 68%
                  reduction in energy use with the solar water heating system
                  and compares well with the June and July reductions of 63%
                  and 60%, respectively. Consistent findings indicate that the
                  tank and piping insulation has reduced the standby tank losses
                  and improved the solar water system efficiency.  
 In the energy housing unit, three of the 100 watt incandescent
                  lamps that were on the evening four-hour timed duration were
                  exchanged for 25 watt compact fluorescent lamps on June 4th.
                  This change did appear to have a small effect on the cooling
                  load in the energy housing unit. The relative cooling energy
                  used by each of the housing units from June, 2002 through August
                  2002 showed a small change. The percentage reduction in cooling
                  energy used by the energy housing unit increased from about
                  30% to 38%. However, it is difficult to isolate the effects
                  of the improvements in the solar water heating system insulation
                  and the effects of the compact fluorescent bulbs. In any event,
                  these effects appear to be much smaller than that produced
                  by the hot water system changes.  
 Year
                  3 Side-by-Side Monitoring Results: 
 | 
 
  Figure 51  Heating
                          season consumption  
                          and savings for side by side study
                      of  
                      Energy Star Manufactured Housing.   | 
 
 
Heating
                    system savings (2001 to 2002) were a remarkable 70% during
                    Phase 1. Cooling energy season savings were 36%, less than
                    heating but still very substantial. The combined heating,
                  cooling, and water heating savings were 52% for a 9-month period. (Figure
                  51) 
 In
                    addition to the energy monitoring effort, NCA&TSU
                  researchers investigated the feasibility of replacing the conventional
                  framing/envelope used in manufactured/industrial housing with
                  alternative systems. Included in this evaluation, was an analysis
                  of the energy impact of using aerated autoclaved concrete (AAC)
                  flooring systems and structural insulated panels (SIP) to supplant
                  traditional wall and roofing  
                  systems. The economic viability
                  of using AAC blocks for structural skirting /foundation around
                  the model units also was evaluated.  
 Analysis’ results
                  determined:  
 The best manufactured home energy performance can be achieved
                      using the SIP wall and roof systems with the AAC plank. This
                      performance can be further enhanced with an R-8 unvented
                      crawl space. Though a manufactured home performs best with
                      these alternative systems, the cost to include them may not
                      make economic sense.  
-  AAC planks can be designed to replace both the steel frame
                      and flooring systems for HUD code manufactured housing units
                      and modular units. These planks also can be modified to incorporate
                    built-in insulated ducts. 
 
-  AAC planks are pre-manufactured and require less assembly
                      labor than a typical stick framed unit, but including the
                      plank flooring would increase framing costs by 28%. The heavier
                      weight of an AAC system might exacerbate high framing costs.
                      Similarly, comparative analysis results found that replacing
                      a conventional framing system with a SIP system would increase
                    framing costs by 66%. 
 
-  At the current prices for energy and wood products, neither
                      the AAC plank system nor the SIP systems are as economically
                      effective as improvements in the current conventional HVAC
                      systems, steel and wood framing, sheathing systems, and air
                    barriers with respect to improving energy performance. 
 
-  The use of AAC planks has the potential to be economically
                      viable in the modular housing market, especially if used
                      with sealed crawl space foundation systems, where their improved
                    resistance to moisture degradation would be very important. 
 
-  SIP wall and roof systems also could prove to be economically
                      viable if the price of wood energy increases, and the SIP
                    manufacturing costs decrease through large volume purchases. 
 
-  The
                        proposed AAC planking system presents a system that is
                        significantly less affected by water and moisture degradation
                        and may be effective in reducing manufactured housing units’ susceptibility
                      to flood damage. These systems also are not susceptible to
                    termite attack. 
 
-  The
                        savings from reduced transportation damage from greater
                        durability and increased floor system stiffness were not
                        addressed in this investigation. It wouldn’t take
                        many days of damage repair (at about $300/person-day for
                        personnel costs related to transportation) to vastly improve
                    the economics of these alternative systems.
 
 
 
- Portable Classrooms
 
 
 Project Overview  
 This is primarily a WSU (with subcontractors Oregon and Idaho)
                  and Pacific Northwest National Lab (PNNL) task. Other partners
                  include FSEC, UCFIE, the State Energy Offices of Oregon and
                  Idaho, school districts in Portland, Oregon, in Boise, Idaho
                  and Marysville, Washington, regional utilities, manufacturers,
                  and other stakeholders in the Pacific Northwest.  
 The objective of this task is to promote the adoption of
                  energy efficient portable classrooms in the Pacific Northwest
                  that provide an enhanced learning environment, high indoor
                  air quality, and both substantial and cost-effective energy
                  savings. BAIHP staff focus on four main goals: (1) offering
                  technical assistance to portable classroom manufacturers, school
                  districts, and related organizations, (2) field assessment,
                  monitoring, and analysis of innovative building technologies
                  and energy saving features to determine their value, (3) facilitation
                  of collaborative agreements among regional utilities, northwestern
                  portable classroom manufacturers and materials and equipment
                  suppliers, as well as school districts, and state education
                  departments and their affiliates, and (4) conducting and creating
                  educational opportunities to advance the widespread adoption
                  of energy efficient portable classrooms in school districts
                  nationwide.  
 The experiences working on the energy efficient portable
                  were instructive, particularly in the identification of flaws
                  in portable classroom design. The difficulties that BAIHP staff
                  encountered demonstrate the importance of well-defined commissioning
                  protocols, documentation, and coordination among all personnel
                  that service and install HVAC equipment.  
 Findings:  
-  Portable classrooms in the Pacific Northwest are occupied
                    about 1225 hours per year, or about 14% of the total hours
                    in a year. 
 
-  The
                      average number of occupants in the standard 28’ x
                    32’ portable classroom provide an internal heat of
                    about 480 kWh/year, or 8% to10% of space heating requirements. 
 
-  Most of the heat loss in portable classrooms manufactured
                    after 1990 occurs by air leaking through the T-Bar dropped
                    ceilings, because they have no sealed air/vapor barrier.
                    This newly created phenomenon occurred with the incorporation
                    of the less expensive dropped T-Bar ceiling in place of the
                    more expensive sheet rock used in older portables. Air leakage
                    also is increased because of unsealed marriage lines - now
                    used as a low cost method of meeting the state attic ventilation
                    requirements. 
 
-  Since all portables tested in the project used a simple
                    seven-day programmable thermostat, the HVAC systems operate
                    during vacations and holidays. 
 
-  Energy codes in Washington, Oregon, and Idaho are high
                    enough to make beyond-code envelope measures non cost-effective. 
 
-  Older portable classrooms under removal consideration
                    could be retrofitted with new energy efficiency measures
                    at much less cost than purchasing a new portable classroom.
                    Installing low-E, vinyl framed windows, insulated doors,
                    T-8 light fixtures, and caulking and sealing air leaks can
                    all be cost-effective when refurbishing older portable classrooms.
                    HVAC system replacement in older portable classrooms will
                    be the biggest single cost item, ranging from $4500 to $6500. 
 
-  CO 2 sensors appear to be unreliable as a control strategy.
                    Those installed by field crews and monitored by dataloggers
                    in this study did not match the readings shown by the CO
                    2 sensors which controlled the ventilation systems. 
 
 
 Based on data analysis from years one through four, the following
                  measures were recommended. New portable classroom procurement,
                  setup, and commissioning as well as existing classroom retrofit
                  guidelines produced by the BAIHP study can all be found in
                  Appendix A.  
 Recommendations:  
-  Install 365 day programmable thermostats in all existing
                    portables and specify these thermostats for new construction. 
 
-  In portable classrooms constructed with T-Bar dropped
                    ceilings, install an air/vapor barrier above the T-Bar system
                    on the warm side of the insulation. Completely seal all edges
                    and overlaps. 
 
-  If roof rafter insulation is used, seal the marriage line
                    at the roof rafter joint with approved sealant such as silicon
                    caulk or foam. Make sure there is adequate ventilation between
                    the insulation and the roof. 
 
-  Conduct an audit of older portables scheduled for disposal
                    to determine if retrofitting would be more cost effective
                    than purchasing a new unit. 
 
-  Install occupancy sensors to control the ventilation system. 
 
-  Specify that new portables contain windows on opposing
                    walls. 
 
-  Specify that new portable units contain exhaust fans on
                    the opposite side of the classroom from the fresh air supply. 
 
 
 School
                  Partnerships  
 | 
 
  Figure 52  64Energy
                          efficient portable classroom at Pinewood Elementary  
                      School in Marysville, Washington   | 
 
 | 
 
  Figure 53  Graph
                          comparing heating system 
                          use of the Pinewood control
                          portable (P2-Blue) with the energy efficient portable
                          (P5-Red). Note the energy efficient portable’s
                          high energy use during the Christmas holidays due to
                      incorrectly configured heating system controls.   | 
 
 | 
 
  Figure
                                54  Ventilation
                                system testing  
                                at North Thurston School District.   | 
 
 
An 895 ft 2 portable classroom (P5) was sited at the Pinewood
                  Elementary School in Marysville Washington in August 2000.
                  This unit exceeded current Washington State Energy Code standards
                  with upgraded insulation in the floor, roof and walls, low-E
                  windows, and a sensor-driven ventilation system that detects
                  volatile organic compounds (VOCs). A second portable, built
                  in 1985, and also located at Pinewood Elementary (P2), served
                  as the control unit. (Figure 52.) 
 Energy
                  use comparisons of the two classrooms show that the energy
                  efficient portable used considerably more energy than the control
                  portable. This was attributable to several factors:  
-  Incorrect
                      wiring of the exhaust fan, causing it to run continually.
                      The fan was rewired in 2000 during the summer break. Once
                      corrected, energy use in the portable declined. 
 
-  Incorrect
                      programmable thermostat settings which were not programmed
                      to turn the heating and cooling system off during holidays
                      and vacations. Though energy use was reduced when the portable
                      was unoccupied, use was still excessive (Figure 53). 
 
-  Higher
                      air leakage in the energy efficient portable than
                    the control portable. Blower door testing found 19 
 
                    ACH at
                    50 Pa in the energy efficient classroom compared to nine
                    ACH at 50 Pa in the control classroom. Follow-up blower door,
                    smoke stick, and APT pressure tests indicated that the predominant
                    leakage path tracked through the T-bar ceiling and into the
                    vented attic due to an ineffective air barrier in the energy
                    efficient portable. The control portable contains taped ceiling
                    drywall. 
- No
                        initial HVAC commissioning by the HVAC supplier or the
                        school district. 
 
-  Significant
                      HVAC system alterations (including rewiring, ventilation
                      system VOC sensor replacement with a CO 2 sensor, and modifications
                      to other aspects of the HVAC control system) during 2001
                      by maintenance staff and the HVAC supplier, unbeknownst
                    to BAIHP staff. Calibration testing done by scientists at
                    the Florida Solar Energy Center on the CO 2 sensors showed
                    significant drift in output results. This made data collected
                    virtually unusable. 
 
-  The
                      use of plug-in electric heaters during the winter of 2001
                      by the resident teacher because of room comfort problems.
                    This led to significant room temperature variations and monitoring
                    data showed high plug-load energy use. 
 
-  Poor
                      fresh air flow design with the fresh air intake and exhaust
                      fan positioned so they create a “short circuit” of
                    fresh air, bypassing the students and teacher. 
 
 
BAIHP
                            staff proposed the following recommendations to Pinewood
                          Elementary:   
-  Well-defined commissioning protocols, documentation, and
                    coordination among all personnel that service and install
                    the HVAC equipment. This is a critical component of efficient
                    and healthy classroom operation and should include outside
                    airflow rate measurements to assess adequate ventilation
                    and control testing to insure correct system operation. 
 
-  Design changes to the portable classroom manufacturer,
                    including the use of a structural insulated panel system
                    (SIPS), tighter ceiling barrier and sheetrock ceilings, elimination
                    of the vented attic, and relocation of the exhaust fan to
                    the wall opposite the supply air vent. 
 
-  Removal
                    of current HVAC controls and replacement with both an occupancy
                    sensor-driven control for the ventilation system and a heating
                    system programmable thermostat. Staff also proposed a classroom
                    on/off switch to simplify the system turnoff during unoccupied
                    summer and school vacations. 
 
-  Location of exhaust fans in future portables on the wall
                    opposite the supply air vent. 
 
-  Window installation on opposing sides of the classroom
                    to increase daylight penetration and to assist in passive
                    cross-ventilation. 
 
 
 Based
                  on the above recommendations, WSU researchers worked with Marysville
                  school facility manager and customer representatives from Snohomish
                  Public Utility District to assist them in setting new construction
                  specifications for 13 portable classrooms they will procure
                  during the next reporting period. Marysville School District
                  will specify a completely sealed ceiling barrier, a new model
                  heating/ventilation system, a 365 day programmable thermostat,
                  window placement on opposite sides of the classroom, and exhaust
                  fan placement on an opposite wall from the fresh air supply.  
 Washington Schools - North Thurston School District  
 BAIHP staff also worked with the North Thurston School District
                  to troubleshoot a portable classroom in Lacey, Washington.
                  (Figure 54) The classroom was experiencing high energy
                  use and poor indoor air quality. BAIHP staff tested the classroom,
                  made recommendations including opening the supply dampers,
                  installing a wall side vent to better ventilate the classroom
                  and discussed the specification development process with district
                  staff. The North Thurston School District now is including
                  most of the measures listed in the new procurement guidelines
                  for their future portable classroom purchases. The school district
                  will investigate the feasibility of installing an air/vapor
                  above the T-bar dropped ceiling and will record costs for making
                  these improvements.  
 Idaho Schools - Boise School District Retrofit  
 BAIHP staff located a portable classroom at the West Boise
                  Junior High School in the Boise Idaho School District, occupied
                  by a teacher who was interested in having the classroom monitored
                  and retrofitted. The teacher also is an Idaho State legislator
                  active in education issues, which staff members believe will
                  increase the chances of implementing the final recommendations.
                  (Figure 55) 
 | 
 
 Figure 55 Weather monitoring
                      system installation in the Boise portable classroom.  | 
 
 
BAIHP
                    staff performed a baseline audit, and installed monitoring
                    equipment to track the classroom’s
                    energy use during 2000. In 2001, the classroom was retrofitted
                    with an efficient HVAC system (controlled by CO 2 sensors),
                    lighting, and envelope measures. The classroom was then reaudited,
                  and monitored for the remainder of the year.  
 BAIHP staff worked with Pacific Northwest National Laboratories
                  (PNNL) on the pre- and post-retrofit audits, and installation
                  of the monitoring equipment. In their capacity of  
                  providing
                  energy management services to the school district, the local
                  utility Avista Corporation, collected lighting and occupancy
                   
                  data.  
 Monitoring data indicates a 58% reduction in energy usage
                  post-retrofit. Blower door tests indicate a reduction in air
                  leakage from nine ACH at 50 Pa to five ACH at 50 Pa. Data also
                  revealed that heating use actually increased on weekends and
                  holidays because of lack of internal heat gain and because
                  the HVAC control systems are not programmed to shut off on
                  weekends and holidays. The total retrofit cost was $9,892.  
 Monitored data suggests that the CO 2 sensor that controls
                  the HVAC system is not correctly configured. The system does
                  seem to react to an increase in CO 2 levels early in the day,
                  but does not remain on; CO 2 levels only begin to significantly
                  dissipate after one o'clock PM. BAIHP researchers have noted
                  the difficulty of correctly configuring these sensors in other
                  monitored classrooms.  
 Oregon Schools 
 Oregon BAIHP staff worked with the Portland Public School
                  District to procure two energy efficient classrooms. These
                  were constructed to BAIHP staff specifications and included
                  increased insulation, high efficiency windows, transom windows
                  for increased daylighting, a high efficiency heat pump, and
                  efficient lighting. Staff videotaped the construction of one
                  classroom.  
 Monitoring equipment was installed by PNNL staff. Estimates
                  using the software Energy-10 indicated a total energy consumption
                  of 9200 kWh, or $583 per year at Portland energy rates. Measured
                  results showed the Oregon portable used about 6600 kWh for
                  the monitored period.  
 Incremental costs for the energy efficiency measures were
                  $6,705 over Oregon commercial code, including approximately
                  $2,500 for the HVAC system. This suggests a simple payback
                  of 10 to12 years.  
 Initial blower door tests found air leakage rates of 11.3
                  ACH at 50 Pa. BAIHP staff also identified significant leakage
                  through the T-bar dropped ceiling and up through the ridge
                  vents. Other monitoring results indicated that the same HVAC
                  control problems exist with the Oregon classroom as with the
                  others studied in this project.  
 The
                    Energy Efficient model outperformed code level models in
                    the Portland area. The older the classroom, the more energy
                    consumed. Even when compared with new code level models from
                    the same year, the Energy Efficient model used 35% less energy.
                    Conventional code level classrooms do not include energy
                    efficient measures which greatly increases the unit’s operating
                    costs. Classrooms built more than 10 years ago, use twice
                    as much energy as the efficient model. Those older than 20
                    years consume more than three times the amount of energy.
                    From this study, researches determined that high performance
                    classrooms can save anywhere from $200 to $1000 dollars a
                    year in energy costs compared to older, less efficient portables.  
 A survey sent to teachers and maintenance staff indicates
                  a high degree of satisfaction with the efficient portables;
                  the teachers were most impressed with the improved indoor air
                  quality and increased light levels due to the daylighting windows.  
 Historical Data Collection  
 In Idaho, Oregon, and Washington, BAIHP staff worked with
                  local utilities and school districts to obtain historic energy
                  use data on portable classrooms. This data will be used to
                  compare energy usage from the energy efficient portables monitored
                  in this study.  
 In Idaho, BAIHP staff worked with Avista Corporation's energy
                  manager to collect historic data on 14 portable classrooms
                  in the Boise School District. The classrooms each were equipped
                  with discrete energy meters; as a result, BAIHP staff was able
                  to obtain energy usage data for the past three to four years.
                  A procedure was developed to collect information on portables
                  at each school in cooperation with the physical facilities
                  manager and each school lead. Historic data collection continues.
                  Site visits and walk-through audits are planned for these 14
                  buildings.  
- Duct Testing Data from Manufactured Housing Factory
                      Visits
 
 
Over
                    the past 10 years, researchers at FSEC have worked with the
                    Manufactured Housing industry under the auspices of the U.S.
                    Department of Energy (DOE) funded Energy Efficient Industrialized
                    Housing Program and the Building America (BA) Program (www.buildingamerica.gov).
                  FSEC serves as the prime contractor for DOE’s fifth Building
                  America Team: the Building America Industrialized Housing Partnership
                  (BAIHP) which can be found online at: www.baihp.org. 
Data
                    and findings presented here were gathered between 1996 and
                    2003 during 39 factory visits at 24 factories of six HUD
                    Code home manufacturers interested in improving the energy
                    efficiency their homes. Factory observations typically showed
                    that building a tighter duct system was the most cost effective
                  way to improve the product’s energy efficiency. 
BAIHP and others recommend keeping duct system leakage to
                  the outside (CFM25 out) equal to or less than 3% of the conditioned
                  floor area, termed Qn out. However, most homes seen in a factory
                  setting cannot be sealed well enough to perform a CFM25 out
                  test. Results of many field tests suggest that CFM25 out will
                  be roughly 50% of total leakage (CFM25 total). Thus, to achieve
                  a Qnout of less than 3%, manufacturers should strive for a
                  CFM25 total of less than 6% of the conditioned area (Qn total). 
Researchers measured total duct leakage and/or duct leakage
                  to the outside in 101 houses representing 190 floors (single
                  wide equals one floor, double wide equals two floors, etc.).
                  Ducts systems observed in these tests were installed either
                  in the attic (ceiling systems) or in the belly (floor systems).
                  Researchers tested 132 floors with mastic sealed duct systems
                  and 58 floors with taped duct systems. 
Of the 190 floors tested by BAIHP, the results break down
                  thus: 
For mastic sealed systems (n=132):  
- Average
                      Qn total = 5.1% (n=124); 85 systems (68%) achieved the
                    Qn total ≤ 6% target.
 
- Average
                      Qn out = 2.4% (n=86); 73 systems (85%) reached the Qn out ≤ 3%
                    goal. 
 
 
For
                        taped systems (n=58):  
- Average
                      Qn total = 8.2% (n=56); 19 systems (34%) reached the Qn
                    total ≤ 6% target.
 
- Average
                      Qn out = 5.7% (n=30), more than twice as leaky as the mastic
                      average; 5 systems (17%) reached the Qn out ≤ 3%
                    goal.
 
 
The
                    results show that, while it is possible to achieve the BAIHP
                    Qn goals by using tape to seal duct work, it is far easier
                    to meet the goal using mastic. What isn’t illustrated
                  by the results is the longevity of a mastic sealed system.
                  The adhesive in tape can’t stand up to the surface temperature
                  differences and changes or the material movement at the joints
                  and often fails. Mastic provides a much more durable seal. 
Typical factory visits consist of meeting with key personnel
                  at the factory, factory observations, and air tightness testing
                  of duct systems and house shells. A comprehensive trip report
                  is generated reporting observations and test results, and pointing
                  out opportunities for improvement. This is shared with factory
                  personnel, both corporate and locally. Often, a factory is
                  revisited to verify results or assist in the implementation
                  of the recommendations. 
The most commonly encountered challenges observed in the factories
                  include: 
- Leaky supply and return plenums
 
- Misalignment of components.
 
- Free-hand cutting of holes in duct board and sheet metal.
 
- Insufficient connection area at joints.
 
- Mastic applied to dirty (sawdust) surfaces.
 
- Insufficient mastic coverage.
 
- Mastic applied to some joints and not others.
 
- Loose strapping on flex duct connections.
 
- Incomplete tabbing of fittings.
 
- Improperly applied tape
 
 
Duct system recommendations discussed in this report include: 
- Set duct tightness target Qn equal to or less than 6% total
                    and 3% to outside.
 
- Achieve duct tightness by properly applying tapes and sealing
                    joints with mastic
 
- Accurately cut holes for duct connections
 
- Fully bend all tabs on collar and boot connections
 
- Trim and tighten zip ties with a strapping tool
 
- Provide return air pathways from bedrooms to main living
                    areas
 
 
Summary of BAIHP Approach to Achieving Tight Ducts in Manufactured
                  Housing: 
- Set
                      goal with factory management of achieving Qnout<=3%
                    using Qntotal<=6% as a surrogate measurement while houses
                    are in production.
 
- Evaluate current practice by testing a random sample of
                    units
 
- Report Qntotal and Qnout findings; make recommendations
                    for reaching goals
 
- Assist with implementation and problem solving as needed
 
- Evaluate results and make further recommendations until
                    goal is met
 
- Assist with development of quality control procedures to
                    ensure continued success
 
 
Finally, duct tightness goals can be achieved with minimal
                  added cost. Reported costs range from $4 to $8. These costs
                  include in-plant quality control procedures critical to meeting
                  duct tightness goals. 
Achieving duct tightness goals provides benefits to multiple
                  stakeholders. Improving duct tightness diminishes uncontrolled
                  air (and moisture) flow, including infiltration of outside
                  air, loss of conditioned air from supply ducts, and introduction
                  of outside air into the mechanical system. Uncontrolled air
                  flow is an invisible and damaging force that can affect the
                  durability of houses, efficiency and life of mechanical equipment,
                  and sometimes occupant health. With improved duct tightness,
                  manufacturers enjoy reduced service claims and higher customer
                  satisfaction, while homeowners pay lower utility bills, breathe
                  cleaner air, and have reduced home maintenance. 
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